ย 

The U.S. Navy and Air Force stand to save more than $2 billion after jointly developing an engine modification that will keep critically important aircraft flying for years.

The two services and industry worked together to develop and field a modification to CFM Internationalโ€™s CFM56-2 (F108) engine, allowing them to restore exhaust gas temperature margins, increase fuel economy and extend their time between overhauls from 10 to 15 years.

The CFM56 engines are used on the Navyโ€™s E-6B Mercury command and control aircraft and the Air Forceโ€™s C-135 series tankers and reconnaissance aircraft. The E-6B is managed by the E-6B Airborne Strategic Command, Control & Communications Program Office, PMA-271.

CFM International (CFM), the engineโ€™s maker, is scheduled to receive the Federal Aviation Administration (FAA) certification of the engine modifications by the end of May, Navy officials said.

โ€œAs incredible as these achievements are, both the Navy and the Air Force were struggling to reclaim lost engine efficiency,โ€ said Andy Noble, the Navyโ€™s CFM56 propulsion engineer. โ€œIn our case, only half of the engine life was being regained after the first overhaul. We could not gain back the performance we saw with the original engine build. Even with improved build techniques and test cell procedures, we would be doing well to recover half of the original time on wing between overhauls.โ€

About four years ago, the Navy CFM56 engine team, having exhausted all known means to reclaim lost engine performance, asked CFM to make design improvements.

That effort paid off and resulted in Jeff Bauer, the CFM program manager, submitting a proposal in April 2009 for commercially proven design improvements used in newer models of the CFM56 engine family, Noble said.

โ€œThe recommendations proposed by CFM addressed the Navy and Air Force concerns of reclaiming lost engine efficiency, as well as introduced fuel efficiencies that would bring additional benefits,โ€ he said.

Realizing incorporating these improvements were too costly for the Navy to implement on its own, the E-6B CFM56-2A engine manager, Gerry Cronkrite, pursued a collaborative effort with Tim Misner, the Air Forceโ€™s CFM56-2B (F108) engine lead program manager. Their coordination resulted in a plan that could be advantageous to both services.

Empowered with this information, the Navyโ€™s E-6B program manager here and the Air Forceโ€™s Headquarters Air Mobility Command provided authorization to pursue the design improvements in early 2010. They then combined efforts to share the costs of flight and ground testing as well as gathering the necessary data required for FAA certification.

Over the next few months, the updated engine would be tested, overhauled and tested again four times. This extensive barrage of ground testing helped reduce the amount of flight test time required and provided CFM engineers a controlled environment to capture FAA certification data. When the ground tests were complete, the engine was rebuilt and certified ready for flight tests by Navy and CFM engineering.

To help prepare for the upcoming flight testing, Lt. Stephen โ€œMerleโ€ Haggard, a test pilot at Air Test and Evaluation Squadron (VX) 20 here, recommended flying all test points in the Navy E-6 Level โ€œDโ€ flight simulator. Those simulated flights were done in August and September 2011.

In early December 2011, having met all the readiness review requirements, VX-20 Chief Test Pilot Cmdr. Jason Rider authorized flight-testing to begin. Testing was conducted between Dec. 9 and Jan. 11 through the coordinated efforts of VX-20, Navy Propulsion Engineering and CFM Engineering.

“I was excited and fort